Doug Gardei's Flights | ||
Friday | ||
1.) | EZI-65 | Gardei H200G |
2.) | EZI-65 | Gardei I133R |
Saturday | ||
1.) | Zookeeper | AMW M1350WW |
2.) | Ladyrobin | AMW J370GG |
Sunday | ||
1.) | Hotel Express | Gardei G75-7B |
2.) | Super Black Magnum | AMW K475WW |
![]() I made the decision to attend Nerrf 3 when I decided to attempt my level three certification. With support from Robert DeHate and Paul Robinson, I began construction of my modified PML Ultimate Endeavor. Construction started in April, and the June 22nd date was fast approaching. I was balancing my time with my work, and trying to get the beast done. Everything was done, documentation and all around midnight the morning of. Slept for about four to five hours, got up and finished loading the car. Got on the highway and started headed south. I arrived at the launch site shortly after 9am. I spent a moment walking the line, seeing who was there and checking out the vendors. Then I set up camp and unloaded the rockets from my car. I only brought 4 rockets, and the things I needed to fly them. I brought my EZI-65, Ladyrobin, Magnum, and of course my Level 3 rocket; the Zookeeper. Once everything was set, I started loading rockets. It was a very windy day. Like me, most people were limiting what they wanted to fly. The wind was carrying the rockets to the other side of the treeline, and it was very tedious getting on the other side of the treeline. I only made two flights on Friday. First I put together a 2 grain Green 38mm motor I dubbed a H200 and placed it in my LOC EZI-65. This motor operated at a higher pressure than normal cause the nozzle size I chose was on the smaller side. Apparently, I drilled the delay to short for that chamber pressure and the motor suffered a blow-by shortly after liftoff. Despite that, the flight was cool with its nice green flame. There was no damage to the rocket but the forward bulkhead in the motor was melted.
Saturday was calmer but still windy. I decided to go ahead and attempt my level three, and I wanted to get if off the ground before I do anything else. With Robert DeHate’s help, I got the AMW M1350 White Wolf loaded in my case, and he assisted me with getting the rocket ready. He also provided a parachute since the chute I was promised never arrived. Once everything was ready, I headed up to the Away cell. We slid the rocket onto the rail, and after turning on the camcorder, the rocket was raised into launch position. After arming the electronics, charges, and motor, we walked back to the flight line.
About a half hour later, after traveling the long narrow dirt roads to get to the other side of the tree line, I got to see the damage. The camera section was totaled, including the camera. The fincan was also damaged. Two fins was knocked out of alignment, which caused the body to bulge. The electronics seemed ok. The Pico altimeter lost power, but the G-Wiz reported 7,553 feet. Both Apogee charges went, but both Main Chute charges never went off. Not sure what happened. Post check up showed all the wires were where they were supposed to be. I have a suspicion that the G-Wiz did not function properly judging by the data I downloaded from altimeter after the flight.
I noticed a problem right away. The stand off was a threaded pipe where the threads were on a taper. With the weight of the rocket, the taper was pushing the rocket away from the rail, which I was afraid will cause the lugs to pop off again. So the Pad Manager assisted me by wrapping tape around the rail. I was just about ready to go back to the flight line when the tape ripped, the rocket dropped, and the rail button popped off. It is now ten minutes till waiver is up! I immediately borrowed a pocket knife and screw driver and made a quick fix. It was four minutes till the end of waiver when the J370GG roared to life, sending the Ladyrobin skyward with a brilliant Green flame. Somehow the shock cord between the two sections separated, and the lower section was severely damaged. Saturday was over, and three of the four rockets I brought were no longer flyable. Tim Lear from Wildman Hobbies was offering LOC Lil’ Dithers for 50% off to participate in the Crazy Wildman Dragrace. Nerrfs event was Lil’Dithers with G77 Redlines. I missed out on the event, but I decided to build it in my hotel room so I have something else to fly Saturday besides my Magnum. I also decided to rename the rocket the “Hotel Express.”
I want to thank they guys for letting me launch the Magnum. My tent was a good distance from the RSO table. I had to pass messages up and down the tent line because they said that they were closing the range! I shouted to the nearest person, "Let them know I got another bird coming!" They passed the message down the line. Then I heard over the PA “Please communicate what size rod you need!” Then I shouted "Rail!" "What size?” “Standard!” They left a standard pad up for me and it was not long till my Magnum took off with its K475, reached 3000 feet, and had a near perfect recovery.
Photos by Print Your Hobby and Douglas Gardei. Used with Permission.
Please e-mail me if you want a copy of any video file. |
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